引用本文:常洪莉,王婷婷,程耀泽. 高含硫天然气硫磺回收装置液硫沉积物分析及对策[J]. 石油与天然气化工, 2024, 53(6): 14-19.
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高含硫天然气硫磺回收装置液硫沉积物分析及对策
常洪莉1, 王婷婷1, 程耀泽2,3
1.中国石油海洋工程有限公司海洋工程设计院;2.中国石油勘探开发研究院;3.提高油气采收率全国重点实验室
摘要:
目的 某高含硫天然气硫磺回收装置液硫中出现大量黑色沉积物,进而引发了液硫储罐泵泵轴卡死、过滤网堵塞、硫磺造粒装置性能下降等一系列问题,严重影响到硫磺颗粒正常生产,需追溯其产生原因并提出解决措施。方法 通过元素组分分析、工艺流程分析以及现场实验,对黑色沉积物的形成原因进行分析。结果 分析认为液硫脱气催化剂的注入是造成黑色沉积物的根本原因,液硫储罐泵阴燃是黑色沉积物形成的促成因素。结论 通过采取优化液硫处理操作参数、改善液硫脱气工艺、更换液体催化剂、引进固体催化剂脱气技术等措施,可从来源上消除黑色沉积物,并为现场解决硫生产问题提供操作和调整的参考。
关键词:  高含硫天然气  硫磺回收  液硫脱气催化剂  黑色沉积物  液硫储罐泵  阴燃
DOI:10.3969/j.issn.1007-3426.2024.06.003
分类号:
基金项目:中国石油集团海洋工程有限公司2024年科研项目“150 m水深天然气综合处理平台设计关键技术研究”(202402-0301)
Analysis and countermeasures for sediment in liquid sulfur in sulfur recovery unit of high-sulfur natural gas
CHANG Hongli1, WANG Tingting1, CHENG Yaoze2,3
1.Engineering & Design Institute of CPOE, CNPC Offshore Engineering Company Limited, Beijing, China;2.Research Institute of Petroleum Exploration and Development, PetroChina, Beijing, China;3.State Key Laboratory of Enhanced Oil & Gas Recovery, PetroChina, Beijing, China
Abstract:
Objective A large number of black sediment appeared in the liquid sulfur of the sulfur recovery unit of a high-sulfur natural gas, which led to a series of problems such as the pump shaft stuck of the liquid sulfur storage tank, the blockage of the filter screen, and the performance degradation of the sulfur granulation unit, which seriously affected the normal production of sulfur particles. It is necessary to investigate the causes and develop corresponding countermeasures. Methods The formation causes of the black sediment were analyzed through elemental composition measurement, overall process analysis, and field experiment. Results The analysis results showed that the black sediment originate from the injection of liquid sulfur degassing catalyst, and the smolder of the liquid sulfur tank pump accelerates the formation of black sediment. Conclusions By optimizing the operating parameters of liquid sulfur treatment, improving the liquid sulfur degassing process, replacing the liquid catalyst, and introducing the solid catalyst degassing technology, the black sediment can be eliminated from the source, which can provide the operation and adjustment reference for solving the problems of sulfur production on site.
Key words:  high-sulfur natural gas  sulfur recovery  liquid sulfur degassing catalyst  black sediment  liquid sulfur tank pump  smolder